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通过分析550 kV GIS隔离开关绝缘拉杆频发闪络事故的原因,认为GIS隔离开关绝缘拉杆装配前质量控制不严,装配过程操作不当,是造成事故的主要原因,并提出了相应的防范措施.

By exploring the reasons of frequent flashover accidents of insulating pull rod in 550 kV GIS disconnector, it was concluded that the lax quality control of GIS disconnector insulating pull rod before assembly and improper assembly process are the main causes of accident. Then the prevention measures were proposed.

参考文献

[1] 霍凤鸣,周新伟,甄利,李晓峰.500 kV GIS隔离开关绝缘拉杆放电故障原因分析[J].河北电力技术,2009(04):7-8.
[2] 党向东.断路器绝缘拉杆的可靠性验证[J].高压电器,2010(08):63-65.
[3] 段剑,何子东,霍凤鸣,甄利,李晓峰.550 kV HGIS隔离开关拒动分析[J].高压电器,2010(01):58-60.
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[5] 汪沨;张乔根;邱毓昌.GIS 中绝缘子与电极接触不良时闪络特性分析[J].绝缘材料,2001(01):45-47.
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