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介绍了石钢采用60 t BOFLFVDCC流程生产GCr15轴承钢的工艺实践,重点研究了工艺过程中氧含量的控制,工艺过程为:以60 t氧气转炉作为轴承钢初炼炉,终点高拉碳,控制下渣量≤50 mm;采用高碱度(R≥3.5) CaOSiO2Al2O3渣系进行钢包精炼处理,实现了较好的脱硫和脱氧效果,通过合理的吹氩制度去除了更多的夹杂物;VD处理时真空度控制在67 Pa以下,保持真空时间为10~20 min,VD处理结束后进行吹氩弱搅拌4 min以上,去除了更多的夹杂物,保证了较低的氧含量;石钢施行全流程保护浇注,有效地防止了钢液的二次氧化。最终成材氧的质量分数平均为9.5×10-6,最低达7×10-6,达到了国内先进水平,实现了转炉冶炼GCr15轴承钢的高效、高质、低成本生产。

The GCr15 bearing steel is produced by 60 t BOFLFVDCC route at Shijiazhuang Iron and Steel Company. The key points of the practice are:close oxygen content control on BOF by catching carbon practice, control of the slag carry over during BOF tapping, using CaOSiO2Al2O3 slag with high basicity(R≥3.5) for LF refining,removal ot deoxidization products by effective argon blowing,with further removal during VD process under a vacuum less than 67 Pa and for 1020 minutes and a weak stirring for more than 4 minutes at the end of VD process,protective casting to prevent reoxidation. The average oxygen content of the final products was 9.5×10-6,with the lowest of 7×10-6. The production of GCr15 bearing steel at Shijiazhuang steel is on the domestic top level with such efficient, low cost route.

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