欢迎登录材料期刊网

材料期刊网

高级检索

某油田在商检过程中发现1根965MPa高强度套管外螺纹接头存在裂纹。通过对该套管进行断口分析、金相分析、力学性能检测、化学元素成分检测,认为套管化学成分和力学性能符合订货技术要求,裂纹是在工厂淬火之前就产生的轧制裂纹。由于该套管母管切定尺管时没有将母管含轧制裂纹的端头彻底切除,在随后加工外螺纹之后进行探伤检验也没有发现该带原始轧制裂纹的套管,致使该含裂纹的套管发给油田。为防止存在裂纹的套管下井,对该批套管逐根进行了探伤检查。建议工厂加强该工序质量检查,并将该工序作为驻厂监造的重点环节之一。

It was found during inspection that there was a crack on the pin of 140ksi high strength casing.It is considered that the crack was rolling crack occurred before quenching in mill based on crack and fracture analysis,metallography,mechanical property test and chemical component check.The crack was still in the casing pin because it was not removed from the mother pipe and was not found later during threading and NDT.In order to prevent such casing with crack from running down well,it was inspected for all the casing in the batch.It is suggested that factory should strengthen quality inspection in the working procedure which is also one of the keys for supervision.

参考文献

[1] 吕拴录,骆发前,康延军,迟军,贾应林,吴富强,谢又新.Φ273.05 mm套管裂纹原因分析[J].钢管,2010(z1):17-20.
[2] 吕拴录;龚建文;卢强 等.HA6C井提升短节外螺纹接头断裂原因分析[J].机械工程材料,2001,35(02):86.
[3] 吕拴录,李鹤林,冯耀荣,赵新伟,袁鹏斌,王新虎,邝献任.V150套管接箍破裂原因分析[J].理化检验-物理分册,2005(z1):285-290.
[4] 许峰,吕拴录,康延军,杨成新,李怀中,秦宏德.井口套管磨损失效原因分析及预防措施[J].石油钻采工艺,2011(02):140-142.
[5] 吕拴录,袁鹏斌,魏茂质,宋顺平,唐飞,吴天灵.73.0 mm EU J55油管短节断裂原因分析[J].理化检验-物理分册,2008(12):715-718.
[6] 吕拴录,康延军,刘胜,李怀中,余冬清,吴富强.井口套管裂纹原因分析[J].石油钻探技术,2009(05):85-88.
上一张 下一张
上一张 下一张
计量
  • 下载量()
  • 访问量()
文章评分
  • 您的评分:
  • 1
    0%
  • 2
    0%
  • 3
    0%
  • 4
    0%
  • 5
    0%